Early U.S. Navy Afterburner Development Efforts
Part 3a: McDonnell Aircraft Corporation – Initial Proposal and Development
by Paul J. Christiansen
Published 1 May 2026
| Part 1: Ryan Aeronautical | Part 2a: Solar Aircraft: Early Design and Development |
| Part 2b: Solar Aircraft: Production Design and Development | Part 2c: Solar Aircraft: Production Testing and Continued Development |
| Part 2d: Solar Aircraft: Production Testing and Continued Development | Part 2e: Solar Aircraft: Final Testing and Program End |
| Part 3a: McDonnell Aircraft: Initial Proposal and Development | Part 4: Westinghouse Aviation Gas Turbine Division (in process) |
McDonnell Aircraft, St. Louis, Missouri
11 January 1947: The first two XF2D-1 BuNo. 99858 flights (858-1, 858-2) of 14 and 17 minutes duration occurred. No major mechanical or aerodynamic difficulties were encountered. Both left and right engines were Westinghouse X24C-4B.
4 March 1947: McD sent a new proposal, “Proposed Investigation of Performance Characteristics of XF2D-1 Airplane with Special Afterburner” to BuAer, as a possible amendment under Contract NOa(s) 6130.” This proposed development and installation of “short, light-weight” afterburners (AB). A three-angle drawing of the modified aircraft with the proposed ABs installed was included. McD argued that while thrust augmentation with ABs in the F2D appeared to have great promise, the current AB designs in test were not good solutions. They were too heavy and too long. This was because they included complicated flame holders and long ducting that resulted in increased weight. Such an airframe weight addition behind the main wing would shift the airframe center of gravity beyond the XF2D-1’s permissible limits and create stability issues. McD proposed developing a light and short AB especially designed for the F2D that would conform to the airframe weight and balance requirements. McD had been doing ramjet development for helicopter blades and felt such a “short stack” was possible using a new and novel flameholder design that would permit a much shorter body. Their preliminary investigations had been focused on a ramjet flame holder that consisted of a series of steps in the flow chamber wall. It had shown promise in sustaining the flame front satisfactorily at very low pressure losses. In spite of the much higher gas velocities encountered in a turbojet, they felt that reasonably good stabilization of the flame front could be maintained in the proposed configuration. McD proposed a study and a series of model tests to establish the required dimensions of the step-type burner. A blower would supply heated air to the model at velocities equivalent to the actual engine. After establishing the required dimensions, full size ABs would be built for use on test engines at the Westinghouse facility in Philadelphia. After any required alterations were completed on the ground test stands, two ABs would be constructed for use on the XF2D-1 airplane. They recommended that, in the interest of expediting the development, all requirements and regulations pertaining to Navy inspection be waived for all articles except the final units designed for use on the actual airplane. The procurement form listed the “purpose of the procurement was to increase the static thrust approximately 30% to improve further the performance of the XF2D-1 airplane. Two units were needed for one airplane.” The quoted cost was $99,753.00.
7 March 1947: BuAer volunteered the XF2D-1 wind tunnel model to the NACA to assist them in studying the difficulties being encountered with twin inlet turbojet configurations at high Mach numbers. The experimental aircraft’s flight program could be adjusted to include any specific data required by NACA for correlation purposes.
13 March 1947: The preliminary performance test reports on the XF2D-1 stated that the radio antenna mast created a violent “buzz” that prevented using Military power at any altitude. Above 15,000 ft, compressibility effects limited the speed to that obtainable using slightly more than Normal power. The true airspeed reached at both 15,000 and 20,000 ft was 540 mph. Inconsistent results were obtained and were caused, apparently, from variations in engine performance from day to day. Overall, the type appeared to be far superior as a carrier fighter than any other (jet) model observed to date, but it was recommended a maximum effort be made to raise the limiting Mach number to 0.85.
21 March 1947: McD sent in their cost proposal (MCR No. 42A) to change the XF2D-1 design to switch from using the X24C-4A, which used oil mist lubrication, to the X24C-4B, which used solid oil lubrication. Gross AB weight would go up 188.2 lb (including 40 lb of ballast), Vmax at sea level (SL) would be unchanged. The rate of climb at SL would go down -200 ft/min with the service ceiling going down -420 ft. The take off distance would go up 35 ft, the stalling speed would be increased by 1 mph and the wave-off rate of climb would go down -55 ft/min. The unit cost for each airframe was $6,202.00.
14 June 1947: Contract Amendment 2 was issued covering the AB development, construction of test units, two flight capable units and installation in a single XF2D-1 airframe. It added Item 12 to Contract NOa(s) 6130 for an estimated cost of $87,490.29 and increased the contract fixed fee by $5,249.42 for a total price of $92,739.71. All work was to be complete not later than one year from the date of the amendment.
28 June 1947: Contract Amendment 3 was issued covering modifying one XF2D-1 airframe into a 600-mile combat radius fighter. The airframe to be used was BuNo. 99859. The total estimate cost plus fixed fee was to be $55,161.00.
11 July 1947: McD asked BuAer for any data they had on the performance of cooling air ejectors for turbojet engines. They had found that the data they had located was meager in volume and often presented conflicting data. The requested ejector data would be required in the development of the AB for the XF2D-1. They requested that BuAer ask NACA to conduct a program to study cooling air ejector nozzles. A separate memo on the same date showed that McD had met with Dr. G.W. Lewis, NACA Director of Aeronautical Research, and related their need for data on ejector cooling in relationship to their XP-85 and XP-88 projects as well as the AB project. They asked him to assign a high priority to the necessary tests to provide the data.
21 July 1947: BuAer notified McD that the Power Plant Division (PPD) had requested a progress report to date on the AB project and that the report should include the proposed development program details.
13 August 1947: The McD Helicopter Research & Propulsion Division forwarded the first two contract progress reports for AB development, J7-100-1 covering 15 March to 15 April 1947 and J7-100-2 covering 15 April to 15 June 1947 to BuAer. (The reports were not retained in the contract file.)
4 September 1947: McDonnell Contract NOa(s) 6130 Progress Report J7-100-3,
15 June to 15 August 1947
1. AB scale model tests were continued.
2. Negotiations were initiated with Westinghouse Electric & Manufacturing Company for testing the full-size AB in their laboratories.
3. Preliminary design and layout of the full-size experimental AB were completed.
4. Detail drawings and shop work on full-size AB were started.
A. Equipment: The setup was modified from the prior arrangement (See Figs. 2 – 9). This was done to achieve greater exit velocities. The velocity now reached was 850 ft/sec and 10 inHg total pressure at 1,500°F and was considered the best that could be obtained with the available equipment. Although lower than the actual engine, the conditions were adequate for the determination of the flame holding and combustion characteristics of the special step configuration being tested. Higher pressure in the full-scale AB would compensate for the higher velocity to give comparable performance. A water-cooled total pressure rake was constructed to determine the AB exit total pressures.
B. Fuel Injection and Distribution Tests: Initial tests used atomizing nozzles in the center cone and investigation revealed that when the AB became hot, alternate vapor and solid fuel flowed through the nozzles. The vapor lock causing this was eliminated by constructing a hollow center cone with the atomizing nozzles removed. Injection of the fuel through twelve 1/8" tubing fingers was substituted and these gave good fuel distribution and were used for the remaining scale tests.
C. Outer Shell Tests: The unknown time interval between ignition and complete combustion made scale model combustion chamber length analysis to simulate a comparative length performance in the full-size AB difficult. If it was insignificant, the scale model should give an external flame length comparative to that of the full-size AB. Three different combustion chamber lengths were tried; the shortest showed considerable external burning, the medium and longest showing very little and of nearly equivalent lengths. This gave a 36" minimum full-size AB length and a 54" length from turbine flange to exhaust outlet. All subsequent tests used the long model combustion chamber AB in order to prevent adding any secondary effects to the test data.
D. Outer Flame Holder Tests: The 0.4" diameter tube flame holder reported on previously gave good burning, but had excessive pressure loss. Some was due to the scale effect of the over-scale burner used in the model, but other flame holder configurations were tested. The surface type upstream step gave equally good combustion, but a high cold flow pressure loss similar to that of the round ring flame holder. The AB shell was heated to a red-white color from the step to the exit nozzle. The shielded upstream step flame holder gave performance similar to the surface type, except that the AB shell did not become red-white hot until approximately 12" downstream of the flame holder. The downstream step flame holder gave good burning with a similar high cold flow pressure loss, as in the other types. Starting was difficult at low fuel flows and the range of fuel flows for smooth combustion was narrow. This was the only outer flame holder model showing lean and rich mixture limits. An annulus flame holder gave similar burning and skin temperatures, but a lower cold flow pressure loss than the shielded upstream step flame holder.
E. Diffuser cones and inner flame holder tests: The short diffuser cone with a 0.45" downstream step flame holder was tested without an outer flame holder in order to obtain the cold flow pressure losses caused by the diffusion and inner cone flame holder. The pressure loss was found to be 2.44%. Burner tests in this configuration were satisfactory with good burning being obtained over a wide fuel flow. Flame flickering occurred at low fuel flows and a loud resonating noise occurred at rich mixtures. The shell was red hot only at the exit nozzle. The long diffuser cone with a 0.25" upstream step was tested in a similar manner to the short cone. The pressure loss was 2.37%. The downstream step diffuser cone was expected to have less pressure loss in the full-size AB. Burning tests gave similar results to the short cone.
31 October 1947: McDonnell Contract NOa(s) 6130 Progress Report J7-100-4,
15 August to 15 October 1947
1. Scale model tests of basic AB configurations were completed.
2. A clamshell exit nozzle scale model was constructed.
3. Equipment for clamshell exit nozzle flow test was designed and was being constructed.
4. Negotiations for testing in the Westinghouse Electric & Manufacturing Company laboratories were continued.
5. Detail drawings of full-size AB test models were completed.
6. Construction of full-size AB test model was continued.
A. Two scale model ABs were constructed and tested, design based on previous reported results.
B. A new water-cooled total pressure rake was used to obtain the final pressure loss data. A new installation location removed the effect of the exit cone pressure loss and the radial components of velocity from the data.
C. The one-third scale Model A-1 (Fig. 11) AB had the best overall performance to date. It had good combustion over a wide range of fuel/air ratios. The external flame length was 4 to 6 times the exit diameter and blue-orange in color. Pressure loss, corrected to full scale conditions, averaged 4 – 5%. The Model A-2 AB proved that it had good possibilities when scaled to full-size at an extra short length. The pressure loss was slightly higher than the Model A-1. Burning tests were inconclusive as the scale size flame holder steps were too small to hold the flame. It was considered likely that the full-sized AB would have the flame front starting at the step and combustion would be completed in the shorter overall AB length.
E. Analysis of Clamshell Nozzle Flow Constants: The full-size AB would incorporate a clamshell type variable nozzle. The model had different coefficients of discharge and velocity at different openings and these had to be determined by calibration. The resulting curves could be used in analysis of afterburner performance. A 1/3 size scale clamshell nozzle was selected for calibration using the method shown in Figure 10.
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| Fig. 10. Clamshell Exit Nozzle Calibration Method | Fig. 11. 1/3 Scale Clamshell Eyelid Nozzle for Calibration Testing. |
Full Size Afterburner: Detailed design of the full-size AB test models had been completed. The basic design was similar to the scale size Model A-1 with several interchangeable flameholder step sizes and combustion chamber lengths added. An electrically actuated clamshell exit nozzle would permit rapid changes in exit area. A full-size AB similar to the A-2 was being designed. Constructed of stainless steel, Type 309 was selected because of its good high temperature properties and availability. Alternate nozzle parts made of Inconel “X” would also be tested.
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| Fig. 12. Scale Model A-1 Test Afterburner Showing Parts | Fig. 13. Scale Model A-2 Test Afterburner Showing Parts |
8 January 1947: McDonnell Contract NOa(s) 6130 Progress Report J7-100-5,
15 October to 15 December 1947
1. The clamshell variable exit nozzle was calibrated.
2. The fabrication of (Full Size) models A1-5000 and A1-5100 ABs was completed.
3. The fabrication of an alternate forward section for the A1-5000 AB was started.
4. The fabrication of an alternate clamshell exit nozzle of Inconel “X” material was started.
5. Ignition test on the scale model was completed.
6. Test work at Westinghouse was started.
A. Calibration of the variable exit nozzle was completed in accordance with the method described in the prior report. Figures 14 and 15 depict experimental equipment set up.
Fig. 14. Calibration Blower and Mass Flowmeter Measurement Equipment Fig. 15. Scale AB Clamshell Calibration Equipment B. While all scale testing did not require direct ignition, the hot gases entering the AB causing automatic ignition, direct ignition was added to preclude problems when full‑size AB testing began. A sparkplug with a 0.125" gap was added in each of the inner and outer flameholder steps of Model A-1. The entering gas temperatures were reduced until self-ignition no longer occurred. At that point, with temperatures between 600 – 980°F, either sparkplug gave instantaneous smooth ignition at low fuel flows. Below 600°F, there was a delay in the ignition between steps if only one sparkplug was used. At a normal blower temperature of 120°F without any preheat, satisfactory electric ignition occurred. When only one sparkplug was used at the ambient temperature, the opposite step would not ignite.
C. Preliminary setup for the full-scale tests was started at Westinghouse on 9 December 1947, with instrumentation of one test cell completed. Calibration of the engine was started but was delayed when hot spots were observed on the turbine. A clogged fuel nozzle was discovered.
D. Full Sized Test Models:a. The test models A1-5000 and A1-5100 were completed and delivered to Westinghouse for testing.
b. An alternate forward section of the A1-5000 AB was being fabricated. The construction was similar to the original section except that 0.043" thick, Type 347, stainless steel sheet was used instead of 0.064" thick, Type 309.
c. An alternate clamshell exit nozzle was being fabricated of Inconel “X” steel.
13 February 1948: McD requested that BuAer allocate a model J34 engine to the Solar Aircraft Company to assist in their development subcontract in connection with the McD AB contract. Test of the AB was dependent on the availability of such an engine for the work to be accomplished. If such an allocation could not be made, permission was requested to use one of the J34s allocated to the F2H-1 (the letter “H” now replacing the prior contractor letter “D” to avoid confusion with the Douglas airframe designation) production contract of NOa(s)-9022. If approved, McD requested BuAer take the necessary actions to replace the engine on that contract.
4 March 1948: McDonnell Contract NOa(s) 6130 Progress Report J7-100-6,
15 December to 15 February 1947
1. The initial phase of static performance tests on the A1-5000 and A1-5100 AB configuration was completed.
2. The A1-5000 AB with 1" flameholder steps was redesigned for further testing.
A. Initial testing was delayed due to hot spots in the engine, rectified by 29 December 1947.
B. Comparisons of data taken before and after the AB tests indicated that the AB caused no unusual deterioration of the engine performance.
C. A cold flow (now termed “dry”) calibration test with the A1-5000 installed with 3/4" flameholder steps, 53" long showed unexpectedly low thrust losses of 3% at 12,500 rpm and an SFC increase of 3.5%.
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| Fig. 23. Engine WE002062 Calibration Test Results | Fig. 24. Engine WE002062 with A1-5000 AB Attached, Dry Calibration Results |
Ignition: The worst internal flow conditions were used for ignition tests. The fixed exit was 18 ¾" and produced low outlet temperatures and high airflow. No AB starts could be obtained above 4,000 rpm. With 1" flameholder steps, spark ignition range was extended to 12,000 rpm at the outer step and 11,500 at the inner step. It was concluded that a sparkplug located at the downstream corner of the step was a satisfactory ignition method. Addition of an independent fuel supply to the sparkplug was expected to raise the smooth ignition range to the required 12,500 rpm.
D. Burning tests began on 5 January 1948 and continued until 4 February. The excessive noise produced delayed testing and required muffling. Only 3 hours of AB burning were recorded during the period.
Total Pressure Recovery: The water-cooled total pressure rake operated satisfactorily for several tests, but finally failed at the tube welds. Vapor pockets had likely formed and permitted overheating.
Combustion: The tests indicated a need for a larger step than the ¾" step being tested. Ignition was difficult and burning was unstable at high rpm. When the 1" inner flameholder step was substituted, the flame held at the step and displayed good stability over a wide range of fuel flows. Several successful tests were made with the ¾" outer step and 1" inner step combination. The exit flames were red-blue in color at the AB exit and extended out in a cone shape for approximately 5 feet. Most of the external flame was transparent blue in color. Tests with 1" inner and outer steps indicated that configuration was the most stable burning of those tests.
Performance: No maximum performance data was obtained during the initial tests. The AB flow rate was limited both by inadequate fuel pressures and the small exit diameters used on the AB.
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| Fig. 25. Initial Test Data for McDonnell A1-5000 AB |
Construction: The initial construction of the first A1-9000 AB caused some delays. The flange gaskets on the combustion shell burned out after short running times. Flanges buckled and caused warping of the shell because of the differential thermal expansion. Simple design changes would eliminate the failures. Structural failure of the inner step flange was caused by fatigue failure of three fuel injection tubes. These likely failed as a result of vibration of the inner fuel manifold which was not anchored firmly. It was observed that the nose contour of the streamlined island supports caused a sharply diverging airflow which deflected the fuel from the nearby nozzles and caused a cool streak in the section of the combustion chamber behind the islands. The initial tests on the A1-5100 AB were unsatisfactory. No stable burning above 5,000 rpm could be obtained. Increasing the flame holder step size might correct the problem, but because the A1-5000 was performing so well, it was decided to postpone the A1-5100 tests until a later date.
1. Fabricate redesigned AB.
2. Start second phase of testing at Westinghouse on 1 March 1948.
3. Continue design of AB for flying tests:a. Modify cooling shroud design as indicated by test results.
b. Design two-position exit nozzle.
c. Design bellows type joint to permit +/-2° AB misalignment.
d. Design control system.
e. Design a quick disconnect joint.
f. Design AB mounting lugs.
[End Part 3a of the Early US Navy Afterburner Development Efforts – McDonnell Aircraft Corporation]