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In the Winter 2007 Issue of
Early Intercooled Merlins
In the aero-engine literature, accounts and accolades abound of, and for, the 60-series Rolls-Royce Merlin engine with its prominent box-shaped intercooler radiator sitting atop the two-stage, two-speed supercharger
The use of an intercooler on the 60-series Merlins was the first instance of
such a component being incorporated on a production engine from R-R but prior to
this, a lot of thought and quite a bit of practical work had been applied to the
subject using engines with single-stage superchargers.
Chrysler's 1,000 HP Recuperated Turboprop
Anticipating the switch to gas turbine powerplants for future aircraft designs, Chrysler had begun preliminary studies for a company-funded gas turbine engine. The analytical work was assigned to engineers Sam Williams and John Jones, who had earlier designed and tested an axial-flow supercharger for the XI-2220 engine. They studied a variety of configurations, all of which featured a heat-exchanger to recover heat from the exhaust gasses as a means of improving fuel economy, the major shortcoming of early gas turbine engines.
Aero Engine Drawings by Frank Munger
The Mawen Bi-Rotary Engine
Incorporated in Paris, France, Mawen also maintained offices at 500 Fifth Avenue in New York City. Mawen was one of several concerns in the 1930s that had purchased the patent rights for the a class of engines invented by Ignacz Sklenar of Hungary. Sklenar applied for a patent for his first bi-rotary engine on 19 May 1914. A bi-rotary is a type of rotary engine with relative motion between a cylinder row and an encircling annular valve member. With Sklenar’s 1914 bi-rotary design, the crankshaft and cylinder row were geared so they rotated in opposite directions at different speeds. Sklenar also left off the tops of the cylinders and the entire rotating cylinder row was encased in a fixed ring. The inner surface of the ring thus formed the tops of the cylinders and had sliding valve intake and exhaust ports and spark plugs built into it. As the cylinder row rotated, each cylinder in turn passed the appropriate stations on the ring for normal four stroke operation. Believing that the bi-rotary engine had potential for use in both military and general aviation aircraft as well as possible automotive applications, Mawen initiated a series of engineering tests to refine the design. By 1938, a seven cylinder Mawen engine of 75 hp and a nine cylinder engine rated at 175 hp had passed French Air Ministry tests and a development contract for three engines of about 1,000 hp had been secured. Development efforts were also simultaneously taking place in the United States. In July of 1937, Professor Andre J. Meyer had signed a contract with Mawen to serve as a consultant. Meyer and his team made improvements to the design, construction, lubrication and durability of the engine.
"Gearing for Gearheads" Redux
The Packard test set-up followed the nearly universal industry practice of “motoring” two gearboxes of identical ratio coupled input to input and output to output on what amounted to a dynamometer chassis. A constant torque was maintained between the input couplings of the two gearboxes by a twisted torsion bar. The two gearbox output couplings were connected by a torsionally rigid shaft assembly that allowed adjustment of the relative angle between the two output shafts. Test preparation involved preloading the output shaft by “winding” the input coupling torsion bar to introduce the torque required for the particular test. The angular twist in the torsion bar was read by virtue of a fixed degree wheel at one end of the torsion bar and a torsionally unloaded and tubular concentric member indexed at the other end and reaching to the degree wheel to provide a cursor marking.
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