The Lycoming XR-7755
Working Topic 1947
by Kimble D. McCutcheon
15 Jan 1947. The AMC wrote Lycoming regarding Contract No. W 33-038 ac-564 stating that: 1) The AMC was revising its program related to this contract and found it necessary to stop the procurement of an additional engine and on the compounded XR-7755 engine version. 2) AMC was not in the position to extend the basic contract beyond what was then obligated. Contract modifications were being considered that would insure a 50-hr flight approval test IAW AAF Specification XR-28398-A was completed even at the expense of sacrificing other contract items. AMC wanted to eliminate, or hold in abeyance, items pertaining to future development so that remaining funds would go toward this test with a minimum of accompanying development. This might have required modified ratings, if necessary, since the test was to be accomplished with engines and parts then available. More information is available in the Contracts and Administrative Section. [RG 342 RD 2311 XR-7755 Contract W-33-038AC-564 Proposed Procurement & Mods]
18 Feb 1947. During a telcon from Lycoming, Ryder and Pinto (the new Army Air Forces Resident Inspector) advised Blackwood that a propeller nut wrench was needed. The reworked supercharger had arrived along with an injection pump installation drawing. Lycoming intended to install the supercharger and fuel injection pump on engine #101, which was headed back to the test stand. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
26 Feb 1947. Carpenter from Lycoming advised Blackwood that Lycoming had put the work reduction into effect and had stopped building the fourth parts set to the extent possible (i.e., no new jobs were started, but those in process were completed). Engine #101 was on the dynamometer, which was having vibration trouble; the engine was rear mounted, but its front end had to be stabilized. The carburetor was erratic up to 1,600 rpm. The dynamometer bearing had heated up, which was being investigated. The run was about four hours short of completion. Engine #102 was being built up with the new link pin retainer and was expected to be ready to run in a couple of weeks; if problems arose with the #102 run, then new parts would be installed. Reduction gear parts were still 3-4 weeks away. The 3-cylinder test engine was back in its test stand. The new link pin retainer and link pins plated with silver-lead-indium were in. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
Power (bhp) | 4,500 to 5,100 | 4,000 to 4,500 | 3,000 to 4,000 | 2,000 to 3,000 | 1,000 to 2,000 | 0 to 1,000 |
Time (hr:min) | 1:15 | 0:47 | 1:52 | 3:00 | 4:27 | 4:46 |
4 Mar 1947. During a telcon from Lycoming, Ryder and Pinto reported that #101 had been run in to 2,570 rpm and 5,000 hp. Test engineers were fixing oil leaks, and when the run-in was complete a 50-hr test would begin on 5 or 8 Mar 1947. It appeared Lycoming would just get by with a 100°F induction air inlet temperature and no ram pressure requirements, a marginal situation. The hydraulic pump Blackwood had sent had a 16-tooth spline instead of the 12-tooth spline required by the drive; Blackwood advised the test engineers to proceed without the pump. After engine #101 had completed a 15.5 hr run-in, Lycoming provided a chart of time at power. The 50-hr test would begin Monday, 10 Mar 1947. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
4 Apr 1947. During a telcon from Lycoming, Carpenter apprised Blackwood that the dynamometer on engine #102 was down with front bearing trouble and had been for over a week. This had happened during run-in up to 1,900 rpm. The 3-cylinder engine's main drive shaft to auxiliary section driving fuel injector and oil pump twisted off with a torsional failure due to a bad 1 1/2 order vibration at 2,200 rpm. This did not apply to the 36-cylinder engines. The 3-cylinder was reassembled, run in for two hours and failed again with a broken link rod and badly damaged piston due to a piston pin circlip coming out; it had run 22.5 hrs at maximum cruise power. Engine #101 knuckle pins arrived and assembly would start next week. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
9 Apr 1947. Carpenter reported that the 4,000 hp dynamometer bearing pad casing had been off for about two weeks. He expected #101 to be in operation in about a week with the 0.56 reduction gear and torquemeter. The 3-cylinder engine crankshaft and crankcase was serviceable and would be rebuilt next week. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
12 May 1947. Lycoming's C.H. Wiegman submitted preliminary XR-7755-1 dynamometer calibration data, which demonstrated a minimum carbureted bsfc of 0.38 lb/hp/hr with the minimum bsfc points limited by detonation. Lycoming surmised that better mixture distribution and lower-cylinder charge temperatures would be obtained with cylinder head fuel injection. One friction reading at 1,600 rpm and 22 inHgA manifold pressure yielded a friction horsepower of 305. This all pointed to a lower multi-cylinder fuel consumption than was anticipated from single-cylinder data.
rpm | 1,000 | 1,000 | 1,300 | 1,300 | 1,600 | 1,600 | 1,600 | 1,600 |
bhp | 890 | 1,000 | 910 | 1,090 | 1,410 | 1,550 | 1,810 | 1,970 |
bsfc (lb/hp/hr) | 0.390 | 0.380 | 0.420 | 0.405 | 0.405 | 0.395 | 0.385 | 0.380 |
bmep (psi) | 91 | 102 | 72 | 86 | 90 | 99 | 116 | 126 |
damp (inHgA) | 22 | 24 | 18 | 20 | 22 | 24 | 26 | 28 |
[J.G. Blackwood Notes. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Engineering Data.]
Engine #101 was coming off the propeller stand for inspection after 50-hr endurance test. Pinto was helping try to figure out a way to mount a Curtiss controllable propeller on the 0.56 reduction gear, which had a No. 70 shaft and a No. 80 nose. The problem was how to mount the electric propeller brush holder housing onto the nose bolt flange. Pinto had ruled out the existence of an experimental adapter and was hoping to rework a No. 80 nose casting to work. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
Test Engines Time at Power | ||||||||
---|---|---|---|---|---|---|---|---|
imep at rpm | 264 at 2,800 | 241 at 2,500 | 155 at 2,200 | 143 at 1,600 | 90 at 1,300 | Misc | Period Time | Total Time |
Eng No. SC-215-3 Time | 0:00 | 2:54 | 3:14 | 1:45 | 0:00 | 12:01 | 19:54 | 250:06 |
imep at rpm | 231 at 2,600 | 205 at 2,300 | 155 at 2,200 | 143 at 1,600 | 80 at 1,300 | Misc | Period Total | Total Time |
Eng No. 3C-645 Time | 0:00 | 0:00 | 0:00 | 0:00 | 0:00 | 0:18 | 0:18 | 118:01 |
XR-7755 Time at Power | ||||||||
Rating, Power Range (hp) | Takeoff, ≥ 5,000 | Normal, 5,000 – 4,000 | High Cruise, 4000 – 3,000 | Medium Cruise, 3,000 – 2,000 | Low Cruise, 2,000 – 1,000 | Misc < 1,000 | Period Time | Total Time |
XR-7755-101 Time | 0:00 | 0:00 | 0:00 | 31:28 | 6:50 | 5:08 | 43:26 | 118:00 |
XR-7755-102 Time | 0:00 | 0:00 | 0:00 | 0:00 | 0:00 | 0:00 | 0:00 | 22:30 |
XR-7755 Total Time | 140:30 |
X-7 Fuel Consumption | XR-7755-102 Performance | XR-7755-1 Minimum Fuel Consumption |
[J.G. Blackwood Notes. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Engineering Data.]
2 Jul 1947. In a Lycoming telcon, Carpenter related that the 0.56 reduction gear had been mounted on the dynamometer and run-in up to 1,600 rpm. It had then uncoupled due to pinions being stripped from their carrier. An oil hole lubricating the pinions had become misaligned during assembly; this problem was only applicable to the 0.56 reduction gear. It would be rebuilt as soon as possible. The 3-cylinder engine had been rebuilt with old connecting rods but no added weights. This was equivalent to new rods in the 36-cylinder. Lycoming planned to run it 50 hrs at full power, 2,600 rpm and 5,000 equivalent hp. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
26 Aug 1947. Carpenter reported the engine #102 would be ready to test with new rods in about a week. The 3-cylinder engine would be running at week's end with full-floating pins. In fatigue tests past 10 million cycles, over 1 in² silver came off the unloaded side; Lycoming was making up bronze bushings. The 36-cylinder engines had logged between 130 and 135 hours. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
Speed | bsfc | Power |
---|---|---|
1,800 rpm | 0.40 lb/hp/hr | 2,300 hp |
2,000 rpm | 0.41 lb/hp/hr | 2,700 hp |
2,200 rpm | 0.415 lb/hp/hr | 4,000+ hp |
1 Oct 1947. In a Lycoming telcon, Don McKay reported the engine #101 was being assembled for endurance running and would be complete in about two weeks. Engine #102 was on the dynamometer undergoing runs to establish its knock limit. A scavenge out tube leak had caused a fire with damage apparently only to the ignition system. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
13 Oct 1947. Carpenter telephoned to report that the one bank of master rod link pin bearings had started to crack. Although not stated, these were apparently in #101, which had recently been rebuilt. This engine had only been run to 4,000 hp at 2,300 rpm. New rods with floating pins were prescribed. The 3-cylinder link pins had accumulated about 20 hrs, 11 of which were at takeoff power. Its pins were satisfactory. On an unspecified engine, about 6 hrs into a 50-hr test, a coolant jacket cracked at a coolant output fitting. A new bank design included a gusset to reinforce this area on all banks. The test would be resumed next day. In a later report, the coolant pump had cracked with 9 hrs left to go. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
The other engine (presumably #102) was on the dynamometer and would be run early next week. Its run-in would be up to 5,000 hp, along with other calibration activities. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]
17 Dec 1947. Carpenter reported that link pins were satisfactory and that a secondary balancer quill shaft had broken, but running continued. This presumably referred to engine #102. [Penciled notes by J.G. Blackwood. RG 342 RD2311 XR-7755, 1943-1948: 503-602 Conf and Tel Notes.]